10-02-2005, 12:54 AM
Weeeelllll another week is making its way through. I know it is only Saturday but I just wanted to empty the camera and share with the world.
So we dig out the spare engine and look her over...
![[Image: wMTA4NDgxNzZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgxNzZzNDEzZGZkMzF5NTQx.jpg)
![[Image: i=wMTA4NDgxODZzNDEzZGZkMzF5NTQx]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/i=wMTA4NDgxODZzNDEzZGZkMzF5NTQx)
Looks ok on the outside...a little rust but oooook.
The turbo and intake came off like a breeze, the first one ever NOT to break a bolt. This is a good sign.
Next is to remove the valve cover...here is where it gets fishey. On top of the #3 exhaust valve...
![[Image: wMTA4NDgyMDZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyMDZzNDEzZGZkMzF5NTQx.jpg)
I wonder what could cause this? We turned the cam and noticed that the lifter was seized...so I figured maybe that was it..OFF WITH IT'S HEAD
SWEET GOD!!!!
![[Image: wMTA4NDgyMTZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyMTZzNDEzZGZkMzF5NTQx.jpg)
Up close of the carnage!! "It had a little knock" he told me
![[Image: wMTA4NDgyMjZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyMjZzNDEzZGZkMzF5NTQx.jpg)
![[Image: wMTA4NDgyNzZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyNzZzNDEzZGZkMzF5NTQx.jpg)
KAPOW!!!! And that wasn't even the coolest part...
![[Image: wMTA4NDgyODZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyODZzNDEzZGZkMzF5NTQx.jpg)
So yeah...no we don't have an engine for the omni...but its ok. At least we have a bangin' turbo and T2 intake for the tona...
![[Image: wMTA4NDgzNTZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgzNTZzNDEzZGZkMzF5NTQx.jpg)
That WG actuator was my big project for today. Made from a 85' T1 "large can" and the bracket from a T2 can. I used a turn buckle to make it longer...and adjustible :thumbup:
![[Image: wMTA4NDgyMzZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyMzZzNDEzZGZkMzF5NTQx.jpg)
The little can will push open at 14PSI, however it has the mount I needed. This mod goes for like $80 on the net if you have someone else does it.
![[Image: wMTA4NDgzMzZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgzMzZzNDEzZGZkMzF5NTQx.jpg)
The newly cleaned intake is standing tall, polished ridges and the purdy vac manifold. Also cleaned out the fuel rail, the injectors, and re-o-ringed it all.
![[Image: wMTA4NDgzODZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgzODZzNDEzZGZkMzF5NTQx.jpg)
She comes out tomorrow!!! Anyone wanna' come hangout and help?
So we dig out the spare engine and look her over...
![[Image: wMTA4NDgxNzZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgxNzZzNDEzZGZkMzF5NTQx.jpg)
Looks ok on the outside...a little rust but oooook.
The turbo and intake came off like a breeze, the first one ever NOT to break a bolt. This is a good sign.
Next is to remove the valve cover...here is where it gets fishey. On top of the #3 exhaust valve...
![[Image: wMTA4NDgyMDZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyMDZzNDEzZGZkMzF5NTQx.jpg)
I wonder what could cause this? We turned the cam and noticed that the lifter was seized...so I figured maybe that was it..OFF WITH IT'S HEAD
SWEET GOD!!!!
![[Image: wMTA4NDgyMTZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyMTZzNDEzZGZkMzF5NTQx.jpg)
Up close of the carnage!! "It had a little knock" he told me
![[Image: wMTA4NDgyMjZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyMjZzNDEzZGZkMzF5NTQx.jpg)
![[Image: wMTA4NDgyNzZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyNzZzNDEzZGZkMzF5NTQx.jpg)
KAPOW!!!! And that wasn't even the coolest part...
![[Image: wMTA4NDgyODZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyODZzNDEzZGZkMzF5NTQx.jpg)
So yeah...no we don't have an engine for the omni...but its ok. At least we have a bangin' turbo and T2 intake for the tona...
![[Image: wMTA4NDgzNTZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgzNTZzNDEzZGZkMzF5NTQx.jpg)
That WG actuator was my big project for today. Made from a 85' T1 "large can" and the bracket from a T2 can. I used a turn buckle to make it longer...and adjustible :thumbup:
![[Image: wMTA4NDgyMzZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgyMzZzNDEzZGZkMzF5NTQx.jpg)
The little can will push open at 14PSI, however it has the mount I needed. This mod goes for like $80 on the net if you have someone else does it.
![[Image: wMTA4NDgzMzZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgzMzZzNDEzZGZkMzF5NTQx.jpg)
The newly cleaned intake is standing tall, polished ridges and the purdy vac manifold. Also cleaned out the fuel rail, the injectors, and re-o-ringed it all.
![[Image: wMTA4NDgzODZzNDEzZGZkMzF5NTQx.jpg]](http://www.we-todd-did-racing.com/wetoddimage.wtdr/wMTA4NDgzODZzNDEzZGZkMzF5NTQx.jpg)
She comes out tomorrow!!! Anyone wanna' come hangout and help?
Jeff Morrison - Used Car Manager
Woodstock Garage, Inc.
Chrysler - Dodge - Jeep - RAM
Current Stable of Mopar Junk
57 Chrysler Windsor 4drHT - 67 Dodge D100 Short Bed Step Side - 71 Dodge Challenger - 91 Chrysler Lebaron LX 33k mile Survivor - 91 Dodge Dakota V8 - 05 Chrysler Crossfire Roadster - 08 Ram 2500 Cummins
Woodstock Garage, Inc.
Chrysler - Dodge - Jeep - RAM
Current Stable of Mopar Junk
57 Chrysler Windsor 4drHT - 67 Dodge D100 Short Bed Step Side - 71 Dodge Challenger - 91 Chrysler Lebaron LX 33k mile Survivor - 91 Dodge Dakota V8 - 05 Chrysler Crossfire Roadster - 08 Ram 2500 Cummins

